This is my tale of trying to cut some 6061 aluminum to make an aluminum version of a push button depth stop for my Wen benchtop drill press.
I bought a 4" x 6" x 3/4" thick piece of 6061 aluminum from Amazon. From this I cut the body of the depth stop. I also have a 5/8" diameter rod of aluminum I used to make the button for the depth stop from.
Some web research found recommendations for feed speed (17-24rpm), plunge speed (6"/minute), depth/pass (0.03") and bit RPM (13,000) to use when cutting aluminum. My CNC uses a variable speed Dewalt router that can be set at the recommended speed. The other variables I can set for each toolpath in the CNC software I use (Aspire from Vectric.com).
My first try was to cut the perimeter and center hole of the press button body from the 4" x 6" block. I set up the job to cut the part near one corner of the block. The bit I used was a 3/16" spiral upcut end mill. Two sides of the cut were 1/2 the bit width from the edge. The other 2 sides were full width cuts through the aluminum block. I thought all was going fine until about halfway through the aluminum. At that point I started hearing more chatter from the bit as it made the full width cuts through the block. With 1/8" or so to go the chatter was so bad that I had to stop the cut. I took the block off the CNC, then cut the part free from the block using my band saw. I then used a spiral flush trim bit on my router table to trim off the remaining aluminum from the bottom edge. I held the part with a c-clamp as I fed it through the flush trim bit. The bit speed was also turned down to about 13,000rpm.
First attempt |
With a night to contemplate what had happened I decided to try again the next day. It had been full width passes and ramping down that my CNC had trouble with. The conventional profile cuts had deflected toward the part.
For my second attempt I started with a block only 1/8" larger than the final part. I rough cut out the body block from a machined corner of the original block using my bandsaw.
No perimeter passes would be full width. To avoid having to ramp into pocket cuts for the center hole I pre-drilled a 1/4"d hole (using my drill press) through where the pocket was to be cut.
Holding the block in place for the cuts started with a t-track bolt up through that 1/4" hole. A lock washer under a nylock hex nut held the block down tight to my spoil board. To make sure the CNC cuts didn't spin the block while cutting it I separated the cuts into unique toolpaths for each side. While any side was being cut I clamped a block against the opposite side. All profile toolpaths were climb cuts, and only through 1/16" off each side. Twenty two steps were used to get through the 3/4" thick block. All cuts were climb cuts so that any deflection would be away from the part rather than toward the part.
Once the perimeter was cut I took it off the CNC. Now I could clamp the part in my low profile vise to cut the center hole. Starting each pass in the center 1/4" hole I had no need to ramp down between passes. When done I again measured the part and found it to be within .01" of the intended size. The hole was perfectly centered as it was supposed to be.
Part with hole in top and side. |
Conical Springs. |
I tried again, only now moving my low profile vise to the vertical jig so I could better clamp the aluminum rod in place.
Depth Stop Collar Assembled |
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